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So we took it back to my house and unwrapped it from its mold. The mold had charred somewhat, especially the centre board slot, but nonetheless it retained its shape extremely well. The 150 plus dry wall screws did their job and no lead leaked from any part of the mold - so that was quite satisfying.
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Bottom line - the keel looks to be fine with a few pock marks on top where the molten lead continued to bubble, but this will probably be removed when I slice off the top of the keel.
The lesson learned were
1) refine the tap so that the lead is directed down into the mold - the pressure at the tap is quite high, presumably due to the weight of molten lead and tended to splash around, so we had to reduce to the flow to a slower rate.
2) Mark the level on the mold to where the lead needs to be poured - we poured extra since the mold didn't look full enough and I couldn't be sure if some lead had just escaped or leaked underneath. 3) The lead looked to be somewhat discoloured - as if heated higher than necessary - not sure if that made any significant difference, but may have reduced the bubbling and gurgling of the lead when it was in the mold and possible lead to increased charring of the mold.
The mold could have possible managed one more pour, but since the first was deemed a success I consigned the mold to the role of fire kindling.
Finally, I now have the task to cut the top inch or so off the keel, please feel free to comment on the best tools for the job.
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